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LongRunner's Mini-review Collection DISCUSSION

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Re: LongRunner's Mini-review Collection DISCUSSION

Postby Behemot » September 6th, 2021, 6:40 am

Depends how does it work there, here they won't give you that tariff unless you meet certain criteria, provided with electrician audit report.

But yeah, with direct heating, you can get up to 20 hours off-peak here, and also the peak price is only very slightly higher than off-peak. It's considered that households with direct heaters consume so much that they have better grid utilisation factor plus with such high consumption it is slightly because of politics too (there's been some support for electric heating by the end of 90s when they were finishing Temelin NPP as better and cleaner energy source, and once ppl went for it, it's still hundreds of thousand sites who would than have to pay fortune for electric heating, was it not regulated so much).

BTW that De'Longhi, isn't that that coffee-maker maker? :D
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Heater/appliance temperature measurements

Postby LongRunner » October 6th, 2021, 10:21 am

Here are those I've taken to date, which include:
  • 10 fan heaters (8 with wire elements, 2 with PTC ceramic elements)
  • 4 convectors (3 with an additional blower)
  • 1 oil-filled (albeit with an additional small fan heater; will add measurements for a more "orthodox" type if I get an opportunity) and 1 micathermic column heater
  • 1 radiant heater (not to express the actual radiant heat itself though; this is just trivia)
Other appliances include 2 clothing irons, 1 electric frypan, 3 hair-dryers and a hair straightener.

Temperatures of surfaces (as opposed to airflow) are measured with thermal paste at the contact point, for accuracy.
(The cheap white silicone/zinc oxide type is fine for this, as heat density there is nothing compared to CPUs/GPUs which can put heating elements to shame.)
Attachments
Heater temperature data.ods
(33.52 KiB) Downloaded 1075 times
Appliance temperature data.ods
(26.81 KiB) Downloaded 1262 times
Last edited by LongRunner on October 8th, 2023, 2:23 am, edited 9 times in total.
Reason: Added Electrafire and HS25F
Information is far more fragile than the HDDs it's stored on. Being an afterthought is no excuse for a bad product.

My PC: Core i3 4130 on GA‑H87M‑D3H with GT640 OC 2GiB and 2 * 8GiB Kingston HyperX 1600MHz, Kingston SA400S37120G and WD3003FZEX‑00Z4SA0, Pioneer BDR‑209DBKS and Optiarc AD‑7200S, Seasonic G‑360, Chenbro PC31031, Linux Mint Cinnamon 20.3.
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Rice cooking data

Postby LongRunner » November 13th, 2021, 11:25 pm

It's now in a spreadsheet (ODS); both my current (TS12, RC5600) and previous (TS5) units are included here. Not that any of it really comes as a surprise…
Attachments
Rice cooker operation data.ods
(23.42 KiB) Downloaded 972 times
Last edited by LongRunner on November 9th, 2023, 12:52 pm, edited 1 time in total.
Reason: Added TS12
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Molded plug problems persist

Postby LongRunner » February 5th, 2022, 12:57 am

When I wrote my 7th round of micro-reviews, I was pleased enough with the construction of the DēLonghi HSX3324FTS (and related models) that I gave it (albeit with some generosity) a Bronze award. I've had no joy with the molded plug, unfortunately; that already ran warm when I got it, and now (still only 5 months later) gets quite hot. The next time I operate it, I'll have a cup of water ready and dip the pins in after unplugging; if it boils, the original plug will go and I'll fit another Clipsal 439S. This puts the award status right on the brink; while the plug is easy enough to replace, that doesn't mean I'll relax my standards.

So the annoying trend of molded plugs being the weak point on portable heaters (at least since the Chinese/Taiwanese took over making cordsets) continues.
(To be clear, this weakness exists regardless of the connected appliance; it's just that most of the rest don't draw enough current for long enough to notice it, at least until the connection is almost gone.) Incidentally, while writing round 10 (including the Ariston N11HPLWAU), I saw that PATELEC lists DēLonghi among their customers; that doesn't say which DēLonghi appliances use them, but why not use them on a heater where it matters most of all?
(Especially a relatively expensive line-up anyway; DēLonghi already have the HCM2030 as their budget model, at least comparatively…)

I've been pondering why the connections degrade so easily, and mechanical stress seems to be the factor largely provoking it; this can be from flexing the cord near the plug, or (and harder to avoid) the force exerted on the pins from plugging and unplugging (not that I've done a crazy amount of that). The latter situation can be even worse in many molded NEMA plugs which don't even have a rigid plastic frame inside (relying on the overmolded PVC alone for retention).
In rewireable plugs, there's usually a bit of slack in the wires which can comply with small (sub-mm) movements (computery types can think of QFP vs. BGA); that said, my handful of older Australian/European-made cordsets have held up pretty well. Perhaps also more-rigid pin retention helps…

Anyway, for what it's worth, the HSX3324FTS's cord is of the same make as other recent DēLonghi heaters I've seen; the cable itself (which is reasonably flexible, at least) from I-Sheng, the plug from Lian Dung (even though I-Sheng make countless complete cordsets themselves). This time it's the basic 1.0mm² though (previous models I've seen, even the HCM2030, had 1.5mm² cords which may well have mitigated the connection weakness by brute-force), despite still having 1.5mm² internal wires (silicone double-insulated, type FG4G4) in the 10A paths (suggesting that either the cord size was dropped as an afterthought, or possibly the internal wires are shared with the 120V 1500W HSX3315FTS; though I'm not sure that's an option when I don't see any UL/CSA marks on them :huh:).
In a way the Mainland plug on my Kambrook KFH660 was "better"; that at least ran cool when new and made the 1-year warranty without getting dangerously hot.
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SU-Z780 repairs

Postby LongRunner » June 3rd, 2022, 2:05 am

New fan and modified controller.JPG
New fan and modified controller.JPG (273.63 KiB) Viewed 75105 times
As I mentioned in the micro-review, I indeed went with the salvaged Nidec D08K‑24PH fan. However, I tried a different approach to regulating the supply voltage: Instead of dropping the input to a 7824 with a Zener diode, I decided to rebuild the original control circuit with some modifications.

SU-Z780 fan controller.png
SU-Z780 fan controller.png (30.01 KiB) Viewed 75105 times
Controller.JPG
Controller.JPG (247.07 KiB) Viewed 75105 times
Originally this circuit was powered from a lower voltage, but there's a link that can be removed to disconnect it from there (even though it doesn't cross over any other tracks); I then patched it onto the main +42V (using a solid Cat5e core on the underside). I replaced Q802 with a BD140 on a small heatsink (originally for the 7805 in an early ATX PSU, though unfortunately only made of steel), and Q801 with a BD139 (overkill power-wise, but it's what I have with the correct pinout and doubles as additional anchorage for the heatsink). Preliminary testing with a 12V fan (Power Logic PL80S12M from a Macron PSU) and two 4.7V 1W Zeners (what I had) in series worked OK, although Q802 got quite hot (given the rated 140mA draw of the PL80S12M, it would have been dissipating about 4.2W); I then got some 24V 0.5W Zeners (along with 22V, 20V and 18V versions in case I want to slow the fan down) in my last Mouser order, and replaced C802 (originally 100μF 16V Panasonic SU) with a 220μF 35V Nichicon PW. I also found the matching header as used in the Kyocera laser printer I salvaged the fan from, and installed one in place of the original header. With calculated dissipation down to 1.26W, Q802 stays much cooler now.
(In doing this fan mod, R806 should be upgraded to at least ¼W. If you have a higher original supply voltage, it may even have to be ½W; or you could up its resistance as long as it still provides enough base current for the Q802 replacement of your choice.)

D08K open.JPG
D08K open.JPG (257.95 KiB) Viewed 75105 times
These Nidec D08K fans are also unusually easy to oil the sleeve bearing in; simply twist-unlock the impeller by turning it in reverse while gently pulling it.
After oiling, just insert the impeller and rotate forward to lock back in.

Back.JPG
(scratches were from my rotary tool kicking itself out of the hole while extending it; don't use a handheld drill for the holes if you have a drill press)
Back.JPG (247.71 KiB) Viewed 75105 times
I found that FSP use M5 screws to mount the fans in their PSUs, and if anything they actually give a stronger grip than the usual self-tappers; I bought some other M5 screws (10mm long) and nuts at Bunnings, and since these (made by Pinnacle Hardware) have better threads (without noticeable triangular distortion), they hold stronger still. (Initially I got zinc-plated as normal, but later saw some black versions and got them to match.) In theory M5 screws might be too tight with the stated 4.3±0.3mm mounting hole tolerance (I believe 4.8mm self-tappers are recommended), but I got away with it here (despite the high torque).
In the worst case, you could use a reamer. It seems to me that speed of installation is the only real advantage of self-tapping screws.

Transformer.JPG
Transformer.JPG (316.62 KiB) Viewed 75105 times
The transformer was evidently also replaced observing the bodged mounting, previous screw marks in the bracket, and that the mains wires are soldered straight to the pins (quite ugly, and even with the AMP-In type end reinforcements, I doubt that's up to standard in a metal-cased device which is supposed to be Class II :dodgy:) instead of into a PCB. Also, there are remnants of solder even on the “unused” pin (connection between the primary winding and thermal fuse).
I added a few cable ties to the mains wires for at least a little more peace of mind. A further travail awaited as I noticed the output level bar-graphs dimmed as more segments turned on; however, they're driven by the BA6144 which has constant‑current LED outputs (nominally 15mA each), so what gives?
Transformer connections.JPG
Wire 4 was put where the red arrow points in the previous "repair", I moved it to where the yellow arrow points.
Transformer connections.JPG (303.25 KiB) Viewed 75105 times
HFA1000-25.JPG
HFA1000-25.JPG (289.14 KiB) Viewed 75105 times
It turns out that the supply rail to the meters, which should be around +9V to +13V (comparing the installed 2×33Ω anode resistors with the suggested values), was down around +4.7V; I managed to find a winding giving 2×11.4VAC or thereabouts (was probably an auxiliary supply in the original application) and rewired to one half of that, changing C713 (470μF 16V Panasonic SU) to a 1000μF 25V Panasonic HFA (salvaged from a Compaq-proprietary Hipro PSU years ago) to be on the safe side. I also upped the anode resistors from 2×33Ω ⅛W to 47Ω + 68Ω ¼W (per side) to better-fit the datasheet recommendation.
(I actually found out the hard way that the auxiliary winding's center tap has to be grounded separately, and in hindsight, it would have been possible to put it on the ≈3.8VAC winding to get ≈7.6VAC from the anti-phased half of the auxiliary winding. But I'm not putting the PCBs through another round of desoldering just to change the components back…)
Now the level graphs maintain a nice steady brightness, and also the Super Bass LED (very dim before) lights properly (it has its own current source using discrete components, which was also in drop-out under insufficient voltage).
Observing that the bulk capacitors (C703 and C704) are rated for 71V, the original supply (and hence main secondary) voltage would also have been somewhat higher; output is suggested as 110W peak into 8Ω, but ±42V supplies could only manage that with a perfectly rail-to-rail output stage :silly:.

Feet, CRC.JPG
Feet, CRC.JPG (241.08 KiB) Viewed 75105 times
Potentiometers were cleaned by squirting CRC 2.26 (probably too much of it :blush:) into them and turning end-to-end several times. One of the 4 felt feet (rear-left corner nearest the transformer, possibly due to the heat) was missing, so I replaced them all with some 13×13mm EHI Surface Gard white bumpers (SKU 17582 which doesn't seem to be listed on their site; only larger sizes were available in black, at Bunnings). Based on the feel I guessed they're thermoplastic elastomer (TPE), and later confirmed by sacrificing part of the webbing (it melts on a soldering iron, and unlike PVC would continue burning once ignited).
One of the replacements came off shortly due to inadequate cleaning of the old adhesive (it was hard to remove), so I went at the area with a wire brush (by this point I'm not too fussed about wearing off the zinc).

To get the headphone output down to a safer level for modern headphones (and also lower the output impedance to something reasonable), I added 4.7Ω resistors across each channel out (forming a voltage divider with the original 330Ω 2W series resistors).
In a newly-designed product (if it didn't have the budget for a separate headphone output stage) I would actually use parallel pairs of shunt resistors so that a broken connection there wouldn't cause a totally deafening output volume, but that'd be a bit cumbersome to add as a modification.

Resistor change.JPG
Resistor change.JPG (335.31 KiB) Viewed 75105 times
However, that still wasn't enough; when testing with a sinewave into load resistors, I only got around 10V RMS (12.5W/channel into 8Ω) before clipping (and even instability), and even at that level surprisingly severe crossover distortion appeared on the oscilloscope :wtf:. It turns out that one or both of the power module and transformer replacement (they were probably replaced together given that the original power module was a different type) had messed up the bias network, so it couldn't uphold the required −15V; it uses a Zener diode (D706) fed by a 1.5kΩ 2W (R711) in series with 270Ω ¼W (R702). Observing an example circuit for the SVI3102 (that's about all I can find on it :s), the recommendation is 780Ω (two 390Ω 2W in series). But I was able to remove an identical 1.5kΩ 2W (R553) from the now-unused relay circuit, and tacked their leads together in parallel, also changing R702 to a 33Ω ¼W (although calculating it now, I could have reused one of the original 33Ω ⅛W resistors). If your unit has been altered in the same way, then the neatest resistor change would be to a 680Ω 2W + 100Ω ¼W (or 750Ω 2W + 30Ω or 33Ω ⅛W if you stock E24 values). I also swapped the two AC sense resistors (R555 and R556), which were located backwards compared to the example circuit; but I don't know if that's had any functional change. After that, it manages about 35W/channel into 8Ω (or 45W one at a time) clean, which is as good as it will get with the wimpier replacement transformer (supply rails drop to around ±28V).
Only my load resistors get dangerously hot :mrgreen:, temperatures of everything else seem under control. In theory D706 now has a marginal power rating, but it isn't getting too hot to touch so it might be OK; still, I've included a 1W replacement in my next order to be safe.

One final malfunction showed up after moving house: The input selector changed spuriously, most often returning to the Tape input. I first thought it was from interference in the new location and added 220pF capacitors from the control pins (11..15 and 17 on the LC7818) to ground (pin 16), but that had no effect; I tried bridging out the transformer ground wire (which I thought might have broken, as the ribbon cable suffered a lot of stress during prior repair work) with an offcut of 1mm² flexible earth core (with ferrules crimped on the ends, just for quicker soldering really) from the transformer PCB to the nearest ground link (after grinding off the oxidized tin), but that didn't completely solve matters; I then replaced the entire ribbon cable with an off-cut FDD power lead (shuffled so that its black wires became the two interchangeable 30Vac taps, with yellow ground and red for the preamp winding) and pin header on the board (if I had to buy it I'd have obtained the proper keyed header, but here I used a leftover pin strip from a cheapo Freetronics Arduino kit), after which I found during testing (with the load resistors) that a strange buzzing occured with the main speaker switch off (remote switch on, load resistors on remote speaker terminals), but not with it on.
It shouldn't have done that, since the remote speaker switch takes priority :huh: anyway I squirted yet more CRC 2.26 into it (and the speaker ribbon header for good measure), and so far so good.

Finally I replaced the feet again with some 3M felt pads (circular ¾″/19.05mm, but they do the job anyway), since those elastomer bumpers were gripping my desktop too well and kept tearing the adhesive off :group:.
It now resides beneath Mum's HDD recorder (and second-hand Blu-ray player), so I can actually listen to what little is worth watching on the (“smart”) TV…

In case you're wondering what an original unit looks like, try here.
Last edited by LongRunner on July 3rd, 2023, 8:20 am, edited 3 times in total.
Reason: Final frustrations
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Re: LongRunner's Mini-review Collection DISCUSSION

Postby Behemot » June 18th, 2022, 3:17 pm

The 5V power supply in that power cube does look at least half decent, you'd be surprised what craps you can find out there…besides crap caps, it will most likely work fine for some time.
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Re: LongRunner's Mini-review Collection DISCUSSION

Postby LongRunner » August 26th, 2022, 6:35 am

Behemot wrote:The 5V power supply in that power cube does look at least half decent, you'd be surprised what craps you can find out there…besides crap caps, it will most likely work fine for some time.

I poly-modded it after the initial posting, but it still struggled to get down to 50mV (I don't know what ripple tolerance USB has, although this seems to still compare well to what's available). I've since bought 3 of the non-USB version and updated the post with them.
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